PTQ Q2 2026 Issue

compared to the operat- ing case, are summarised in Table 2 . The stabiliser sec- tion operated normally under the reduced pressure condi- tions, with the following key observations: • The top and bottom temper- atures of the stabiliser column were successfully maintained by adjusting the reboiler steam flow and reflux rate. • Steam consumption, as meas- ured through condensate flow, was reduced significantly from 20 MT/h to 14.5 MT/h. The stabiliser section con- tinued to operate stably at the reduced pressure of 18 kg/cm²(g) and average tem- peratures (top: 78°C, bottom: 193°C) set during the demon- stration run. This resulted in a consistent steam saving of approximately 5.5 MT/h, as shown in Figures 5 and 6 .

Stabiliser section operating conditions

Parameter

Operating case

Low pressure case

Demonstration run

(model)

(plant)

Stabiliser top pressure, kg/cm²(g)

20.2

18.0

18.2

Stabiliser top temp, °C Stabiliser bottom temp, °C

88

76

75-78

201 58.4

189 56.2

190-194

Reflux rate, m3/hr

53.0 14.5

Stabiliser reboiler steam flow, MT/h

20

16

Fuel gas flow, Nm3/h

2,100

2,230

2,200

Table 2

20.5

24.0

Stabiliser top pressure

Steam f low rate

21.0

20.0

18.0

Steam saving ~5.5 MT/h

15.0

19.5

12.0

19.0

9.0

6.0

18.5

3.0

Further analysis confirmed that all product streams met the required quality specifica - tions at the reduced pressure of 18 kg/cm²(g). No detectable HCl was present in the stabi- liser bottom stream, and LPG composition remained within all required limits. Conclusion This study demonstrates that significant energy effi - ciency improvements in refinery column operations can be achieved through optimisation of operating parameters prior to capital-intensive equipment modifications. Using 0.0

Before demonstration run 18.0

After demonstration run

Figure 5 Stabiliser pressure profile

steps. The reboiler (E-01) duty was adjusted to maintain the top and bottom temperatures of the column at the model-predicted values of 76°C and 189°C, respectively. Reflux flow was tuned as required to stabilise the col - umn operation. Samples of FG, LPG, and stabiliser bot- tom streams were collected before and after the pressure reduction for compositional analysis. The key operating parameters during the demonstration run at 18 kg/cm²(g),

an ISOM stabiliser column as a case study, a structured meth- odology was applied, integrat- ing detailed process simulation (in Aspen HYSYS), tray-by-tray hydrodynamic validation, and controlled plant demonstration to evaluate reduced-pressure operation. Optimisation of the stabi- liser operating pressure from 20 to 18 kg/cm²(g) resulted in a sustained steam consump- tion reduction of 5.5 MT/h, corresponding to an energy efficiency improvement of approximately 27%, while maintaining product qual - ity specifications and stable

205

120

Stabiliser bottom temp

Stabiliser top temp

200

110

90

195

Average ~193˚C

80

190

Average ~78˚C

70

185

60

Before demonstration run 180

After demonstration run

Figure 6 Stabiliser temperature profile

82

PTQ Q2 2026

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